After slurry vendor swap on 03/12, re-qualifying tungsten CMP with 10 monitor wafers per the FMEA.
After new conditioner disk on 04/01, re-qualifying all CMP chambers with 5 monitor wafers per the FMEA.
8D D3 · CMP
Containment: lots from chamber held; N wafers under clean_action pending check.
Containment:{腔體} 的批次暫停;{N} 片正在 {清潔動作},等待 {確認}。
Containment: lots from CMP-04 held; 48 wafers under post-CMP re-clean pending residue inspection.
Containment: lots from CMP-09 held; 12 wafers under defect map review pending FA cross-section.
— 真實場景 · Real Scenarios · 共 3 條 —
Email — Pad Replacement Notice
CMP 工程師發給 OPS 跟 PIE,announce 預計的 pad 更換 + 影響。
Subject: [FYI] CMP-04 pad replacement Friday 02:00 — 6-hour downtime
Hi all,
Heads up — CMP-04 pad is at 85% wear (190 wafers since last swap). MRR has dropped from 6000 to 4500 Å/min over the past 30 wafers.
Schedule:
- Pad replacement: Friday 02:00
- Break-in: 30 dummy wafers
- Re-qualification: 5 monitor wafers
- Total downtime: ~6 hours
- Production resumes: Friday 08:00
Impact:
- 8 lots queued for CMP-04 will reroute to CMP-06 and -09 (capacity OK).
- M3 Cu CMP throughput drops by ~25% during the window.
- No customer-facing impact.
Will send qual results before going back to production.
Thanks,
CMP ENG
相關縮寫:MRR · pad · qualification
Conf Call — Dishing Excursion on M2 Cu
Yield review 上 PIE 詢問 dishing 異常,CMP 部門答 90 秒。
Thanks. Quick recap on the M2 Cu dishing excursion.
We saw dishing on the wide Cu pads (≥ 5 μm) hit 48 nm on the last three lots — spec is 30 nm. Effect is localized to the wide patterns; narrow lines are fine.
Investigation:
- All three lots ran on CMP-04 chamber A. CMP-06 and -09 wafers are within spec.
- Downforce log shows an overshoot to 4.2 psi vs 3.5 psi target on the affected lots — controller drift after the 03/12 PM.
- Slurry pH and conditioner are within spec, so they're cleared.
Root cause: downforce controller drift on chamber A.
Containment: chamber A held; downforce controller re-cal'd; 5 monitor wafers ran with dishing back to 22 nm. Released to production after the qual.
Long-term: adding the downforce as an SPC parameter on every CMP tool — currently it's only end-of-run logged. Plus tightening the post-PM qualification window.
3 lots affected, all currently held at the next inspection station. PQA confirms no customer impact yet.
Open to questions.
4.0 Root Cause Analysis — Scratch Cluster on M3 CMP
4.1 Symptom
Scratch defects detected on 18 wafers across 3 consecutive lots (Q3-241 through Q3-243), all post-M3 CMP. Defect inspection shows long linear scratches (200–500 μm) on the wafer surface, concentrated in a single radial sector.
4.2 Investigation Path
- All 18 wafers ran on CMP-04 chamber B during a 4-hour window (08:00–12:00 on 03/14).
- Slurry filter on chamber B inspected; filter housing showed a 2 mm crack — large slurry agglomerates bypassed the filter.
- FA on a fail wafer confirms slurry-particle scratches; no foreign material.
4.3 Root Cause Statement
The scratch cluster is attributed to a cracked slurry filter housing on CMP-04 chamber B, allowing large slurry agglomerates to reach the wafer, confirmed by physical inspection of the filter and FA on the defect.
4.4 Containment
- All 18 affected wafers scrapped after FA confirmation.
- Chamber B held; new filter housing installed; SOP updated to inspect filter housing weekly.
- 100% scratch metrology on all WIP that ran through chamber B in the past 48 hours.
4.5 Long-Term Action
- Filter housing replaced with a stronger material (PEEK).
- FMEA updated to include "filter housing crack" as a failure mode with weekly visual inspection.